So far this morning :
A compression test showed only about 65 pounds ... A few weeks ago , it was at about 80 pounds .
The spark plugs are burning clean , a light tanish coloring . Both plugs are clean , even though the inside plug is insulated from it's wire .
I removed the compression plate cover and plate . I found very tiny bits of what at first looked to be carbon in the bottom of the crankcase , black , but a bit too shiny . Then I took the cylinder off . The bore looks pretty good with a couple places showing a bit of what seems like blow-by and a couple of very light scuffs .
The piston showed much the same as the cylinder , but the scuffs are deeper .
The connecting rod both top and bottom are way too loose . Loose to the point of what looks like the back corner of the rod contacting the crankcase . Neither were loose when I put the motor together a couple years ago . That looseness is most likely due to the lower rod bearing being poor quality .
All that leaves me thinking I'll need a new piston / rings and pin ; bore job and a new rod with QUALITY bearing(s) .
I'm glad I quit running the bike when I did . Much more damage would definitely have followed , otherwise .
Pete .